Hairyarse
New member
Well a productive day off work for me today. This morning I finished installing the handsfree kit to the new stereo, then fitted four of these bad boys;
All works great, I just need to find an ignition switched live as the stereo is currently on a permanent live, anyone know the nearest/easiest one to pick up behind the stereo slot?
Then admired my Turbo in the sunshine on the way back from town
...after which I went to Rob's so we could try and sort my overboost like problem that's been present since not long after buying the turbo. It would only happen on full throttle but power would be cut right back. I had already tested the DME and KLR as per Clark's and they checked out ok, yesterday I borrowed Rob's 3 bar FPR and that made no difference. Today we were going to try Robs AFM and after taking the air box out we noticed the pipe connected to the turbo pipe was a little passed it's best!
...and thanks again to Rob for the temporary fix;
We also noticed one of the T's I had just fitted with the new vacuum lines was cracked so this was changed too.
I then went out and gave her a damn good spanking! OMFG, she works perfectly now (early days but it was spot on!) Soooo quick, I'm gobsmacked and well chuffed. Should turn out to be a relatively cheap fix once I get a permanent hose sorted.
Thanks again Rob, another couple of beer tokens in the kitty for you [8D]
Cheers
Andy [
]

All works great, I just need to find an ignition switched live as the stereo is currently on a permanent live, anyone know the nearest/easiest one to pick up behind the stereo slot?
Then admired my Turbo in the sunshine on the way back from town

...after which I went to Rob's so we could try and sort my overboost like problem that's been present since not long after buying the turbo. It would only happen on full throttle but power would be cut right back. I had already tested the DME and KLR as per Clark's and they checked out ok, yesterday I borrowed Rob's 3 bar FPR and that made no difference. Today we were going to try Robs AFM and after taking the air box out we noticed the pipe connected to the turbo pipe was a little passed it's best!

...and thanks again to Rob for the temporary fix;

We also noticed one of the T's I had just fitted with the new vacuum lines was cracked so this was changed too.
I then went out and gave her a damn good spanking! OMFG, she works perfectly now (early days but it was spot on!) Soooo quick, I'm gobsmacked and well chuffed. Should turn out to be a relatively cheap fix once I get a permanent hose sorted.
Thanks again Rob, another couple of beer tokens in the kitty for you [8D]
Cheers
Andy [