ChasR
New member
It seems that this is not the week for me and cars! My daily snapped a spring and to top it off it looks like it will need a cylinder head refurbished (low pressure on a couple of cylinders). To top it off the 951 is misbehaving.
Basically since it has been my daily for a short while I have been driving it rather carefully (it doesn't help when your daily does the equivalent of over 50MPG!). Anyway, as the red mist descended on me today and I came to put my foot down, the boost gauge swung towards 2 Bar, but with a difference; it hesitated and cut the power fairly hard, initially I was quite surprised and fear the worst. Thankfully the car drove but it did this again for another mile or so upon applying the power.
After that, the car was behaving absolutely fine, pulling very well indeed. What do you chaps believe is the issue? FWIW it's the car in my signature. To my knowledge it is stock bar a Bailey DV30 valve.
I would like to think the car was rebelling against being driven carefully but that may be wishful thinking!
Basically since it has been my daily for a short while I have been driving it rather carefully (it doesn't help when your daily does the equivalent of over 50MPG!). Anyway, as the red mist descended on me today and I came to put my foot down, the boost gauge swung towards 2 Bar, but with a difference; it hesitated and cut the power fairly hard, initially I was quite surprised and fear the worst. Thankfully the car drove but it did this again for another mile or so upon applying the power.
After that, the car was behaving absolutely fine, pulling very well indeed. What do you chaps believe is the issue? FWIW it's the car in my signature. To my knowledge it is stock bar a Bailey DV30 valve.
I would like to think the car was rebelling against being driven carefully but that may be wishful thinking!